Thinking of a rebuild on the engine. I can send the block and heads to a machine shop, I plan on doing a DIY job, I have the tools, just need an engine stand and a cherry picker. Who supplies the best rebuild kit ? Is it worth a rebuild ?
Any tips or advice from those who have successfully...
@LFX1 I used an oil pressure gauge.
But here is the problem I discovered. I previously mentioned that the compression on cylinder #1 was 35 PSI. When I did a wet compression test it rose to 175 PSI. I am assuming that one of the rings are seized and gunked up. The next step is to borescope...
Okay, I will idle the vehicle for a few minutes with the OBD scanner plugged in so that I can monitor the coolant temp until it reaches operating temperature.
I will idle it with the oil pressure tester in. Once it reaches operating temp, I will switch the car off and release the pressure from...
I did an oil pressure test, the results were as follows:
1) Cold Idle: 65 PSI (Workshop manual states: 4 PSI)
2) @3000 RPM: 80 PSI (Workshop manual states: 25-110 PSI)
So it appears that there is high oil pressure issue on idle.
Current Oil is Shell helix HX8 5W40.
The car has a history...
Update:
1) I did a compression test, see results below.
Cylinder 1 - 35 psi
Cylinder 2 - 160 psi
Cylinder 3 - 140 psi
Cylinder 4 - 140 psi
Cylinder 5 - 140 psi
Cylinder 6 - 160 psi
I am assuming that I have a blown headgasket given that there is at least some compression in cylinder 1 and not...
Apparently the best way to remove the sensor is to remove the cooling fan and then work your way in from the top of the engine bay. I don't have a lift and working from the floor could be a serious pain.
That crossed my mind when I was brainstorming possible causes. The oil pressure light did not go on when the engine first misfired. The guys at the shop performed an oil pressure test and told me that it was low, however the warning light was not on, it only illuminated after the car was parked...
The tick is noticeable at idle and when revving the car in Park position. I have not driven the car on the road for a while, if I can recall correctly the sound disappears when I am coasting. I pulled the car out of the garage yesterday and I recorded the ticking sounds, I tried to attach the...
I got an 02 KJ with the 3.7 v6. It previously had a valve seat come loose and had a valve get stuck due to the loose valve seat. A refurbished head was installed a by a "reputable" engine rebuilding company. When the vehicle got back from the shop it had a ticking sound, the guys at the shop...
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