At first I thought that something must've gotten dropped into the intake somehow. However, on closer inspection it seems that a bolt was left inside the cylinder at the manufacturer's facility.
There's no way that bolt made it through the valve without scoring the hell out of it. The bolt was too long to fit through an open valve. You can see that there not a mark in the thing.
Powertrain seems easy enough to work with, not sure how this is going to be handled by them, but they swear up and down that every engine is sim tested prior to leaving the factory floor.
The engine is toast. Need a new block, piston, rod and head at a minimum.
The suckiest part of this whole thing is that it started right up, And for about 3 glorious seconds, sounded like pure heaven.