So long story short I heard a sound which turned out to be a hole in the rubber elbow of my pcv pipe. I think basically it was just rotten and my spongebob filter in the airbox where the crankcase inlet air comes from got dirty enough that the vacuum caused the rotten boot to fail.
I went and got a new pipe from the dealer which ended up being a new part that superceeded my old part. Main difference is just routing. Same diameters and everything. I almost took the boots off the new one to go on the old one but thought maybe they rerouted it for a reason. So I didn't.
So I changed the PCV, installed the pipe and installed a new spongebob filter in the airbox made of a foam filter from briggs and stratton.
Since doing this my MPG has fallen 5 MPG! I am completely puzzled by this.
Anyone else ever experienced anything similar or have suggestions I might not be considering?
Should I change the PCV out again? Disconnect battery to get a reset on the computer? IDK
I went and got a new pipe from the dealer which ended up being a new part that superceeded my old part. Main difference is just routing. Same diameters and everything. I almost took the boots off the new one to go on the old one but thought maybe they rerouted it for a reason. So I didn't.
So I changed the PCV, installed the pipe and installed a new spongebob filter in the airbox made of a foam filter from briggs and stratton.
Since doing this my MPG has fallen 5 MPG! I am completely puzzled by this.
Anyone else ever experienced anything similar or have suggestions I might not be considering?
Should I change the PCV out again? Disconnect battery to get a reset on the computer? IDK